Nice Bruce!
Where is Sharpie Steve's workshop located?
bigBADbenny wrote:Where did you mount the AEM gague and is its output logged?
bosc0 wrote:Nice Bruce!
Where is Sharpie Steve's workshop located?
<GB> wrote:does it work good?
<GB> wrote:i was reffering to the wide band but after looking at that mount thats what i need badly, i get lots of pitch and it bangs a little, i always thought that mount was part of the issue, im not actually sure what mine has lol
also 2 min fit up for mine as i dont have tmic lol
bass_straitener wrote:<GB> wrote:i was reffering to the wide band but after looking at that mount thats what i need badly, i get lots of pitch and it bangs a little, i always thought that mount was part of the issue, im not actually sure what mine has lol
also 2 min fit up for mine as i dont have tmic lol
Well, there you go. I've solved all your issues in one post.
bass_straitener wrote:Thought I'd update my build thread as I've a few more changes are on the way.
Firstly, I've stopped tuning with Matt and Kido Tuning. I've done so because Matt seems to be too busy and I'm finding his customer service is lacking. On his last visit to Melbourne, I spent 1.75 hours in dyno tuning with him at RTR.
The results were not great, hence I'm not posting any graphs, but following the tune my car showed signs of substantial leaning out on acceleration. I've since found some wild values in the throttle tip-in enrichment table which caused these lean spikes. Also I'd asked Matt if he was aware of the popping on decel and gear change fix that MSR and JacksGTB recently posted about. Matt advised he knew what to do and following the dyno run removed some timing from the base timing tables. My laptop had an issue over the next couple of weeks and therefore I couldn't check the tune to see how happy the engine was. I finally got it sorted last week and found IAM was less than 1.0 with significant FLKC. I logged the car via RomRaider to confirm it. I then sent off a couple of emails to Matt, last Saturday, with my results and the tune in question for confirmation of the issue and a fix. To date I have not received a response. I then made the decision on Wednesday after 5 days of no contact to send him a PM ending our relationship. I had been tuning with Matt since July 2012.
I've since had another tuner help me rectify the tune and I've spent the last week logging it daily and amending it to remove all knock. I've now put my Tactrix and laptop down and returned to family life.
Whilst early on Matt was very responsive with information and revisions, he's become more of a marketing machine and his quality has dropped in my opinion. I'll leave it at that and don't wish to turn my build thread into a debate.
The next few weeks will see the car serviced and prepared with DW65c, one step colder spark plugs, and replacement of my second cat prior to a retune in the new year.
I'm sure my retune will conclude my build and I'm hoping to then simply sit back and enjoy the car.
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